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Team Shakesc : Build Diary

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  • #91
    Looks fantastic! Can't wait to see this ramming into stuff!

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    • #92
      Well an interesting Stevenage
      Spur 3 had plenty of push and was fast
      Need the front scoop to help throw some robots about
      At the end of session 1 a tyre came off - not enough screws and need to be pan head
      Fixed that
      Setup for session2 and had dramatic smoke coming from the bot. Crew did a great job of grabbing the robot and racing outside
      After a blast of CO2 worked out it was not lipo but a TZ85a. Once stripped down I could see that one of the motor bolts had come loose jamming the gear and stalling the motor. TZ85a vs NTM 5060. Time for a HK order
      Happy with the day though. Robot shows alot of promise and can focus on fixing various things

      Alex drove Spur 2 and that had a good day after working on strengthening the drive line. It did shed a tyre. Looking at them the rubber is getting end of life. Therefore it starts Sunday with new tyres

      Nuts had a great Saturday , Rory can write that up

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      • #93
        Been a while since I posted on this

        Put a front scoop on Spur 3 and locktite in all the important places. Should be ready to roll

        Started collecting the parts for Heavyweight drive gearbox. Since I was in the US I picked up some Neumotor 8019-150KV
        Its 1.2 Kg of motor goodness
        These are chunky and much more substantial than the Rotomax I was looking at. Once I have finalised the gearbox design I will be off to the local engineering shop for some milling

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        • #94
          those are very nice!

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          • #95
            Those motors leave the Rotomax range for dead! Any thoughts on the ESC you will use with them?

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            • #96
              Many thoughts , havent decided yet. I seem to have started a whole debate in the combat robotics section on FB

              There are the castle mamba xlx and also a China https://l.facebook.com/l.php?u=https...98&h=UAQEuvwCH

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              • #97
                So I see - I am using A Kontronk Kosmik 200 with my 8019 - its powering a weapon so I don't need reverse. The MGM controllers are well made and the tech support is super helpful; they offered to do custom code for me. VESCs are probably borderline for power handling and the guys over here are not sure how they will handle high pole count motors.

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                • #98
                  Had a look at the MGM's, they are nice but pricey [increasingly so with the pound dropping!]. The Castle is looking more of a possibility. Rory was interested in fettling the Aliexpress. For now I will design space that will take either, have enough stuff going on to keep me busy

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                  • #99
                    Thinking about wheels, its been going round and round in my head

                    I made wheels for Spur 3 from Nylon and its was a pain, modified Banebots for Spur 2 and blue tyred jobs for Spur

                    Having seen castor wheels fail spectacularly at robot wars I didnt want to go this way for my heavy. Spent a ton of time trawling round looking for pre-made wheels I found these at TEP Technica Ltd https://www.technicawheels.co.uk/
                    They are worth a look

                    Even better they were about 20 minutes drive away



                    Onto the next bits

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                    • Well, I sat these 2 side by side and the size difference popped out (not surprising)

                      On the left is a bearing support and pinion for a P60 Banebots gearbox. On the right is a BB220 gearbox an pinion
                      Both will be doing the same job but in a feather and heavy. Just hope I dont mix them up

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                      • What motor are you planning to use with the BB220? I found that the rear plate on the older P80 gearbox was hard to use for anything other than the CIM motor and ended up making my own replacement.

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                        • Since I don't have enough pain, misery and frustration in my life I am going large brushless outrunner
                          Start-up torque will be interesting - my usual approach is go big and low KV on the motor then sensorless
                          Be fun finding an ESC that doesnt turn into a toaster and dont get me started on VESC.

                          Did i say I don't have enough pain, misery and frustration in my life

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                          • Got my custom Neumotor shafts back along with my broached gears. I can now do a final measurement check and put the order in for waterjetting
                            This will allow me to put the 2 drive pods together

                            No banana's were harmed in the making of the new shaft

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                            • The work was done by D.C.V. Precision Engineering at Aldershot
                              Andy the MD is a bit of a RW fan Never a bad thing when you are asking for small batches / one offs

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                              • Is this robot going to be the new Tornado/Storm 2? Those look absolutely vicious for drive motors.

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